Havefun and I have successfully completed the Lord Howe Island voyage onboard Morning Bird arriving back in Pittwater at 0300 this morning.
The BBQ on Ned's Beach was great and we met a lot of sailors from all walks of life. The island is really fantastic and worth seeing, even if you don't sail to get there.
Check out the video of the island from the lagoon.
The trip over and return were challenging. It was blowing hard, except when we were becalmed. Lots or nothing. I think we had 48 hours each way with the wind over 25kts average and gusting up to 40 kts for one period. As it was blowing for a long time the fetch was considerable and the seas large and steep. Then last night we had a heavy fog as we came down past Newcastle with the coal carriers anchored offshore.
The conditions also challenged Morning Bird and we had a few problems going over which we resolved as we went. As Havefun said, nothing we couldn’t fix or cope with.
I located a fuel leak at midnight on the 2nd night. It was from a union on the engine lift pump so I waited till morning to work on it. I didn’t want to cross thread the union in the dark or it would have been leaking continuously. At the time we were becalmed and went backwards for 6 hours. We also lost a lot more fuel than I calculated, maybe 20 litres got pumped out of the bilge and we ran out of fuel on the run into the LHI lagoon.
The spray dodger was more rotten than I thought and had a tear before we left. It started to disintegrate on the way over and gave up completely in the gale on the trip back. This made the inside of the boat very wet, but washed away any diesel smell.
A boom fitting parted on the way out for which I had a spare.
We arrived at LHI on the Friday evening but too late to get into the lagoon. We heaved to in what had been a minor gale but which increased to a strong gale overnight. Unfortunately, as we came out of the heave to in the morning a strong gust got the boom (started the gybe in the trough and it went across on the peak) and broke the main sheet block. As the boom swung around it broke the casting on the end of the boom at the goose neck. Havefun did a brilliant job lashing the boom to the mast and sail to the boom in very heavy seas and strong winds. We didn’t try to repair it over there. I have a trisail, acquired for just this contingency, and we used it for the return trip. It should be pretty simple to repair, a job for the next week or so
There were no problems at all on the return trip.
What a great boat and I must say very well set up for these passages. In particular, the Fleming wind vane and the Simrad tiller pilot worked brilliantly throughout. If you are doing longer voyages I highly recommend them (and their variants). The engine and shaft were excellent over many hours work, standfast the fuel leak.
This trip was on my bucket list and I do not expect to do it again. The wife and I have other plans so I will sell MB to someone who will use her as she is intended. Not as a cocktail boat plying sheltered waters but on coastal and longer passages. First, a new dodger and boom fittings.